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    Day 20

    October 7th, 2015
    Today in class my robot broke and I tried to film my end of the quarter video and failed. The string became untied and unattached from the leg. This is an easy fix but something that is a minor set back. I will most likely dissemble the prototype in the following class periods and build the entire chassis as a whole. I also tried to film my end of the quarter video but with several attempts at correct grammar and limited pauses in my speech, I ended up running out of time. Next class I will finish the video and work on the leg. For my documentation, this is a picture of me trying to record my end of the semester video.



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